Spec E46 Build Part V: Suspension

Once again, let’s review the Spec E46 rules regarding suspension:

14. Suspension

1. Shocks must be MCS non-remote reservoir single-adjustable (1WNR).
2. Front springs must be Hyperco 6″ 2.25″ ID 750# part number 186A0750.
3. Rear springs must be Hyperco 5″ 2.25″ ID 850# part number 185A0850.
4. Swaybars may be replaced provided they use stock mounting locations and either individual hole or sliding collar adjustment. Remote-adjustable or blade-type bars are not permitted.
5. Swaybar links may be replaced.
6. Adjustable camber/caster plates are permitted. The three front strut mounting holes and center hole may be notched/trimmed to provide clearance for fitment or achieving full range of adjustment. 7. Any OE-spec E46 non-M3 front control arm may be used.
8. Front control arm bushings and housings may be replaced with a non-spherical bearing.
9. Rear upper shock mounts may be replaced.
10. Rear trailing arm bushings may be replaced with a non-spherical bearing.
11. Height adjustable rear spring adjusters may be added.
12. Rear lower control arms may be replaced.

So with that in mind, I did have a few choices.  Again I went with what seemed to be the most common sway bars, end links, camber plates, and bushings.  I had a set of Rogue Engineering rear lower control arms on hand from my E36 build, so I went ahead with those.

Rear Subframe Complete

 

I’ll start at the rear.  The rubber OE bushings were removed and replaced with PowerFlex Race poly bushings (black.)  The outboard upper ball joint and lower rubber OE mounts were replaced with new OE mounts (no upgrades allowed.)  The lower arms (aka “salad tongs”) were tossed in the trash and the alloy Rogue Engineering arms installed.  Finally, Ground Control articulating weight jacks were added to the upper arms which also received new OE rubber bushings.

For anti-sway bars I went with the Hotchkis Sport kit.  This kit is a 30.2mm front and 25.4mm rear.  It also includes new rear end links, and bracket reinforcement plates for both front and rear.

Rear sway bar and shocks

Of course the shocks, struts, and springs are spec’d in the rules.  For the rear shock mounts (RSM) I used Bimmerworld spherical bearing style mounts, so no rubber to deflect under load.  Front mounts are Ground Control camber/caster plates.  I notched the shock towers to gain additional negative camber and positive caster.

I used the new BimmerWorld solid front control arm bushings (FCAB) for the front.  They’re aluminum with a Delrin insert.  I did have to cut them down to clear the aluminum reinforcement panel.  Just removed the nub that had a threaded boss for the E46M3 brace (not allowed.)

BimmerWorld Solid FCAB BimmerWorld Rear Shock Mount

The rest of the suspension was just about replacing the worn out 220,000 mile original parts.  So new Meyle heavy duty front control arms were installed, eliminating the rubber isolated outer ball-joint.

Bad Alignment = Corded Tires

I knew my rear alignment wasn’t ideal for sure, I had to crank in some extra camber just to get out of my driveway without rubbing the rear arches. The Bridgestone S-04 Pole Positions I had installed when I went to a square setup were much wider than the previous Hankook V12s or Continental Contact3’s that I had, even though all were 245/40R17 (stock rear size.) I even had a slight roll of the rear fenders and slightly raised the ride height. Despite this, I still rubbed on compression when I took the car to MSR-Houston.

The extra negative camber in the rear was more than ideal and was surely upsetting the balance I had dialed in.  More concerning was the apparent toe-in that had come in, so much that it was visible to the naked eye.  Unfortunately I was in the middle of a move from Texas to South Carolina and simply didn’t have time to solve the problem.  Even if I had, I’m not sure I would have completely avoided a little rubbing.  I’m sure the excessive toe-in might have had something to do with it, as the rubbing was at the rear of the arch near where the plastic bumper cover meets the sheet metal.

A trip half-way across the country and several hundred miles of mountain driving later, I was getting close to an upcoming track day at Road Atlanta.  Like any other track driving event, I brought the car in for a good inspection.  I knew I wanted to swap out the brake pads, but I wasn’t expecting to also change tires until I had the rears off and saw this:

Rear Bridgestone S-04 CordedThe rear set of young Bridgestones were corded along the inside tread.  No point in pressing on with these tires.  The fronts still had some life in them, but given that the RE-11s on my M Coupe didn’t fair much better with a good alignment, I decided to change to something else.New Michelin Pilot Super Sports  The Michelin Pilot Super Sports had come down in price and had been very pleased with their performance on the M Coupe at Circuit of the Americas, so I ordered up a set of 245/40R17s.  Interestingly, the S-04s measured out at 9″ tread width and the Super Sports measured 8.5″.  That extra 1/2″ (well 1/4″ on the outside) would surely help my rubbing issue.  They are also 3 lbs lighter and score higher in every category at TireRack.com.

Of course I didn’t want to ruin another set of tires, so an alignment was in order.  I found a local shop that was willing to match my specified settings and seemed comfortable working on a car with camber/castor plates and lower adjustable control arms.  I gave them the print-out from last successful alignment; roughly max castor, -3.2 front camber, minimum toe, -2 rear camber and just a smidge of toe-in.

The image below is a scan of the previous alignment and the latest one.  The upper left figures are from a Firestone chain shop, that was the best I could get out of them.  I’ve since sworn off using them.  I’ve highlighted the variances they dialed in, and this was with proper camber plates that make adjustments very easy.

The lower left is from a speed shop who really were able to get the settings bang-on.  The upper left is the measurements following my fiddling with the rear to fit the over-sized S-04 Pole Positions.  As you can see, there was an excessive amount of rear toe-in.  That combined with the large amount of negative camber is what led to the rear tires cording.

Finally the lower right print-out is from the final alignment.  Ignore the Red/Blue colors, as they weren’t able to adjust the ranges from the manufacturer’s specifications (ie -3.2 camber is outside factory tolerances, but good for track driving.)

Alignment Print Out

The results: well you’ll have to wait for my post on the HPDE at Road Atlanta!

Leaking Power Steering Return Line

So LonelyAt this past weekend’s Cars & Coffee of the Upstate, I was that guy. You know, the guy whose car broke down in the parking lot. The guy who drove in but was trailered off.  Yeah, that guy.

I was debating back and forth on whether or not to take the M Coupe, as I had done during the last event.  I wanted to spend a little time after the show, just to drive around the Greenville area and check out some of the companies I was looking at working for.  That swayed my decision, not wanting to abuse the fresh paint job on the M Coupe any more than I had to.  It had recently left the body shop, where it had spent quite a while getting hail damage repair.  So I opted to take the M3 sedan, not nearly as interesting as the Clown Shoe but still an M Car.

The drive up from Lexington to Greenville (about 1.5 hours) was uneventful, other than being passed by a pack of Corvettes at well over 100mph.  The car performed admirably, just as it had during its long venture from Texas to SC a month ago.  But just as I was pulling into the Michelin HQ parking lot, I started to hear some strange noises and feel some vibrations in the wheel.  It occurred at low speed and high steering angle, uh oh… looks like the pump is going out.  I muscled it into a parking spot, having fully lost power assist by the time I came to a stop.

Hitching a RideI was greeted by a small trail of power steering fluid, dribbled along my path.  I popped the hood to find fluid sprayed under the airbox.  A quick inspection from underneath revealed the culprit: the return line (“Return Pipe with Cooling Coil” in BMW parlance).  The rubber line was kinked and not pressed all the way into the crimp at the end of the coil.  Not good, but maybe I could limp it home.  Just in luck, an AMSOIL salesman had setup a booth in the lot.  I purchased a few bottles of power steering fluid and topped off the reservoir.  I ran the engine, sawed the wheel, and then checked the level again.  Nope, this wasn’t going to work.  I was losing fluid at much too fast a rate.  The return line might as well have been dumping overboard.  This was going to require a tow.  Fortunately my truck and trailer were at the house, and after a call, and a short wait I had my father pulling into the parking lot to retrieve the broken Bimmer.  And being the good stewards of the environment that we are, laid down some kitty litter to sop up the oil.

Leaking Return PipeOnce back home I dug through my stockpile of parts to find a brand new hose, what luck!  I also had a new Bimmerworld AN-fitting hose setup, which I briefly considered, but would require running an aftermarket Moroso reservoir.  I decided this must have been a fluke material failure and to just stick with OEM.  These lines are notorious for seeping fluid at the reservoir connection but this premature blow-out was not the norm.

Changing the line is a fairly simple task, just get the left side of the car slightly in the air for access to the working area.  I also removed the left front wheel for more room, also allowing me to wash all the sprayed fluid out from the wheel well, brakes, wheel, and other parts.  The line must have begun to leak somewhere along my I-26 travels, as it had migrated rearward, thoroughly coating the transmission tunnel.

Jacked Up and Ready to WorkI also scrounged up new aluminum crush washers for a proper fix.  Strange that Real-OEM claims a ’98 M3 requires no washers, yet the PS pump has a recess at the banjo fitting in the exact diameter of said washer.  I elected to install the washers on both sides of the banjo fitting.

Blown Power Steering LineWith the new pipe in place and torqued up, I commenced with the undercarriage bath.  Using some POR-15 Marine Clean, I gave everything a good spray and soak.  I followed that up with the hose and then some time to let it drip dry, aided by a bit of compressed air for under the hood.

Back on went the front wheel and back down on the ground went the car.  With the airbox out of the way I topped off the worst positioned reservoir known to man.  I then cranked her up and cycled the rack back and forth to work the air out.  Everything sounded and felt good, hopefully I dodged a bullet and the pump didn’t eat itself while running low on fluid.  Worst case scenario is that it did disintegrate and then FOD’d the rack in the process.

 

In more interesting news, here’s a totally awesome E38 740i sporting an E39 M5’s S62 V8 and transmission:

S62 in a 7 Series M5 Powered E38

Check the Facebook album for more photos of cool cars!

’98 M3 Sedan Overhaul Part III: Engine, Steering, and Front Suspension

The newly acquired ’98 M3 Sedan has been progressing along nicely, having taken care of the rear suspension and drivetrain already, it was now time to move under the hood.  The engine was already a smooth runner, especially after I solved its intermittent stumbling issue, but there were a couple other items I wanted to address.  Chief among these was preemptively avoiding the dangers of oil starvation under high lateral and longitudinal acceleration (“pulling g’s”).  The M50 family of engines, which this S52 is a member of, have a traditional oil pan.  This is in comparison to the S54’s dual pick-up pan, which was purpose built by the M Division to prevent low oil pressures on the track.  The North American E36 M3’s weren’t fortunate enough to be equipped with a true “M” engine like their European counterparts, which use an S50B32, that incorporate an oiling system nearly identical to that found in the S54.

The negative results of this become immediately apparent even under mildly spirited driving.  After a few hard corners or heavy braking, you can hear the engine develop a loud tick, timed with the RPM of the cam shafts.  This is because the S50/52US use a hydraulic lifter setup, rather than a shimmed (mechanical) lifter like that on the S54.  Why you ask?  Again, we weren’t offered a true motorsports engine, and hydraulic lifters are better suited for daily drivers.  They self-adjust and under normal circumstances are smoother in operation.  However, when oil pressure drops below a certain level, the lifters go out of their specified height and you are left with a rattling valve-train.  This in of itself is not a hugely critical issue, but it is an indicator that the engine is not being properly supplied with oil.  Excessively low oil pressure can and will lead to much more serious problems, like spun bearings, scored piston walls, wiped lobes, so on and so forth.

So what’s the fix?  Well you can certainly go the route I went on my S50 race engine and install the dual-pickup pump and pan from an S54, but that’s pricey for just a daily driver that may get driven hard but a handful of times.  The cheapest alternative is just overfilling the sump with an extra quart or so of oil.  Unfortunately this only mildly stems the issue, the oil is still going to slosh away from the pick-up, you just hope there’s enough extra that the pick-up remains submerged.  I tried this at a recent track-day and found it to only slightly reduce the ticking.  The more proven method is to install a trap-door style baffle in the oil pan.  These baffles are pretty common among track driven cars, in fact my MR2 has one installed on its 2ZZGE.  As the name implies, these baffles use small one-way doors to allow oil to flow towards the pick-up, while restricting its flow away.  Several companies produce baffles for the S50/52, all sharing similar designs; aluminum construction and weld-in.  I did notice that the Turner Motorsports baffle utilized rubber flappers rather than hinged aluminum doors like the others.  I decided for longevity, I’d better stick with an all metal baffle.

I found that the baffle made by Achilles Motorsports was the least expensive option, but still maintained the same design and build quality of the others on the market.  The photo below shows the underside of the baffle so that you can see the “trap doors” in their closed position.

Achilles Motorsport Baffle

Now the big hurdle; getting the oil pan off the engine.  This isn’t a particularly complicated job, but it is very time consuming.  The front subframe, which the engine rests on, resides directly underneath the pan and must be removed to gain access.  That alone is not too difficult a job, it’s all the other items attached to the subframe that add to the complexity.  On the top side, go ahead and get the airbox and alternator cooling duct out of the way, which block your access.  Underneath, the steering rack, inboard ball joints for the lower control arms, and of course the engine itself are all mounted to the subframe.  The X-brace that I had installed must also come out.  Since you are removing the mounting points for the engine, you have to now suspend its weight from above.  This is actually a fairly easy task, using a simple and cheap engine hoist from Harbor Freight.  This hoist is just a beam that rests on the groove between the fenders and engine bay weather stripping.  I pulled the rubber molding up at the leading edge of the fender to allow for easier fitment and also covered the legs of the hoist in painters tape to prevent any scratches.

Engine Hoist Engine Lift Point

The engine should already have a lift point, a steel eye, on the head beside the oil filter housing.  This is where you attach the hoist, then use the large wing-nut to lift the engine slightly so that the weight is off the engine mounts.  Remember that the transmission mounts must still be securely installed to not only carry some of the weight, but also prevent the engine from rotating.  With the subframe no longer under load, I began removing the previously mentioned items.  First to go is the anti-sway bar, which is easy enough.  Next is the power steering pump, which is partly mounted to the oil pan itself.  Of course you must first remove the serpentine belt.  I found that it helped to first remove the engine mechanical fan, allowing for better access to the belt tensioner.  You don’t have to fully remove the fan, just off of the water pump and pushed out of the way.  You don’t have to fully disconnect the PS pump, tying it up and out of the way with some safety wire is an option, but I decided to go ahead and get it completely out of the way.  Part of the decision was based on my discovery that the previous owner had neglected to install half of the needed crush washers on the banjo fittings on both the pump and rack.  My other reasoning was that I intended to completely remove the rack so that I could replace the badly rusted hard lines, therefore requiring a complete drain of fluid.

Ball-Joint SeparatorWith the pump out and on a bench, I went to work on the rack.  The steering rack is mounted to the subframe by two bolts and two nuts, easy.  If you were trying to only remove the pan, and nothing else, you could just swing the rack forward and down, which should give enough clearance to remove the pan.  Since I had other work to complete, I needed to completely remove it, which meant also disconnecting the tie rods at the steering knuckles.  Like nearly all production cars, the tie rods connect to the knuckles by way of ball joints and tapered studs.  Once torqued down, these studs are very difficult to remove.  Yes you could just smack the exposed end with a hammer, but that would most likely destroy the threads and require a new tie rod (the ball joints are permanently mounted.)  You could also use a balljoint fork (aka pickle fork), but this almost always destroys the rubber grease boot.  The better solution is a ball joint separator, which you can see pictured to the right.  The tie rods had been recently replaced by a previous owner, so it was worth the trouble to save them.

Steering Rag JointWith the ball-joints and fluid lines disconnected, you are almost ready to remove the rack.  The last item keeping the rack from just falling out is the rubber joint (aka “rag joint”) connecting the steering column to the rack’s pinion.  This splined joint is secured with bolts and nuts on both the column and rack that pinch the split aluminum down onto the shafts.  Before removing, make sure you make a visible index mark with a paint pen.  This will help you ensure your steering wheel and tires are lined up straight forward after reinstalling.  Of course you still will require an alignment, but this will get you close enough to at least drive the car to the shop.  Like all rubber parts, this joint is susceptible to drying out, cracking, or even tearing.  This can lead to poor steering response among other issues, so it makes sense to replace it while everything is apart.

Now that the steering rack was out, I could begin refurbishing it by replacing those badly rusted hard lines.  But first I took the rack out to the parts washer for a good degreasing.  The hardlines came off without much fuss, as did the plastic breather tube.    All of the lines use o-rings to form a seal, so be sure to lubricate them prior to installation.  I also gave the new lines a good coating of CorrosionX, hopefully preventing future rust issues.

Rusted Steering Hardlines New Hardlines Installed

Loosening Engine MountsBack to the oil pan removal.  With the steering out of the way, I still had the lower control arms to contend with.  But to gain access to the nut holding the inboard balljoints in place, you must first lower the subframe.  This of course means that the engine mounts be disconnected.  Accessing the bottom engine mount nuts is easy, but the top ones require a bit more fuss.  You needn’t completely remove the top nut, but you have to at least loosen them.  I ended up using a very long 1/2″ drive extension and my impact driver to break the nuts free.

With the lower engine mount nuts completely removed and the uppers loosened, I was one step closer to lowering the subframe.  The last step needed was unbolting the lower control arm rear “lollipop” bushing mounts from the chassis so the assembly could drop freely.  A jack comes in handy here, just to lower it in a controlled manner and keep it at a given height.

Now that the engine mounts are out of the way, you can more easily access the nuts that hold the lower control arm balljoints to the subframe.  Again I used the impact driver to zip off the nuts, only it didn’t work entirely as planned.  The driver side came off without any fuss, but the passenger side backed off almost all the way then began to spin the balljoint.  Normally you could just push the tapered joint in harder, thereby giving enough resistance to continue removing the nut.  Unfortunately this didn’t work, and neither did using a large C-clamp to help keep it secured.  I was forced to remove the nut (and balljoint stud with it) by means of a pneumatic cut-off wheel.

Cut off Balljoint Lowering Engine Subframe

This, of course, has ruined the passenger side lower control arm.  I checked the service history of the car to find out that it was still riding on its original arms, so a replacement at this mileage wasn’t completely out of order.  Fortunately I had a pair of brand new Meyle heavy-duty arms on hand, which were ordered originally for my E36 race car.

Finally everything was out of the way, and I could actually begin removal of the oil pan.  The pan itself is held on  to the block with quite a few M6 bolts of varying lengths.  My light-duty 1/4″ impact driver makes quick work of this.  Don’t miss the two bolts that are inside the bellousing, which are accessed through two small holes.  The back of the pan is actually bolted to the lower portion of the transmission’s bellhousing, which utilizes Torx-head bolts.

With all the bolts removed, the pan will still be very securely held to the block by the grip of the gasket and RTV used at the corners.  You may be tempted to use a pry bar to leverage the pan off, but this is a recipe for cracked cast aluminum.  A far better method is a large rubber mallet used to beat on the pan in a few structurally strong spots.  The cast aluminum of the pan is thin in the large flat areas and can be easily cracked, I’d avoid using a deadblow.  Eventually the hold will “pop” and the pan can be dropped.  Careful, as there is still a decent amount of residual oil left in there.

Rally Road Drilled Oil NutNow that the pan was removed, I could take care of another potential problem: the oil pump nut.  Again, this is an issue present on the M50 (possibly other BMW engines of this vintage) where the oil pump nut can begin to loosen and back off, potentially creating a total loss of oil pressure.  There are a few different paths to correcting this, like staking the nut with a center punch or using some red Loctite.  The problem with these methods is that they make it terribly hard to remove the nut for any future maintenance (however slim.)  The other alternative, and the one I used on my S50 race engine, is to use a nut drilled for safety wire.  Several suppliers offer these nuts for cheap, I found Rally Road was the least expensive.

Safety Wired Oil Pump NutThis is a pretty easy job, once you’ve removed the oil pan anyways.  You just have to remember that the nut is left hand thread, I’ve already seen a few photos of other installs which used a negative safety.  (Negative Safety is when the safety wire is run in such a way that it would actually cause the nut/bolt to loosen, rather than stay secure, which is a Positive Safety.)  The nut comes with a length of wire, which was clearly thinner than the standard .032″.  Since I had plenty on hand, I went ahead and installed it with the thicker 32-thousandths.

Back to the oil pan and baffle install we go.  First you must remove the OEM baffle, which is held in by a single rivet that must be ground off.  A 90 degree pneumatic grinder with a sanding wheel made quick work of this.  The OEM baffle, as you can see in the photos below, does very little to keep oil surrounding the pickup.

BMW OEM S52 Oil Pan Baffle BMW OEM S52 Oil Pan Baffle 2

The oil pan must be thoroughly cleaned in preparation for welding in the new baffle.  The pan was just small enough to fit inside my parts washer, where I soaked it with kerosene and scrubbed all the old oil deposits away.  The new baffle fits exactly as the factory version, but must be welded in place.  Since it was aluminum, time to call in a professional.  I dropped the pan off with a welder I’ve used before and had it back the same day for $20.  In the next photos you can see a side-by-side comparison of the OEM and Achilles baffles and finally the new baffle welded into place.

OEM and Achilles Oil Pan Baffles Achilles Oil Pan Baffle Welded

While all this work was taking place, I was also soaking the oil pan bolts in EvapoRust to remove the years of corrosion.  Like I had done with the hardware on the rear of the car, I gave the fresh bolts a good coat of CorrosionX prior to installation to keep them looking new.  The pan was then reinstalled with a new gasket with some beads of Toyota FIPG at the corners where the aluminum timing chain cover and rear main seal cover join the block.

S52 Oil Pan Reinstalled

Front Subframe with new Control Arms and Engine MountsWith the engine’s bottom end buttoned up, I could begin the process of reassembling everything attached to the subframe.  As I previously mentioned, I had new lower control arms to install.  Unlike the OEMs, the inboard balljoints on these Meyle arms had an Allen key socket on the ends of the studs, which should prevent any future issues of spinning ball joints.  The arms also came with new nylon lock nuts, which should prevent them from backing off.

I attached the arms to the subframe while it was clamped to my transmission jack, which would give me a little more control over raising the assembly.  While I was at it, I decided to also replace the original engine mounts, which were beginning to crack and were also heavily rusted.  The passenger side engine mount heat shield was severely rusted, but I had run out of time to order up a new one.  Instead I gave it a long soak in EvapoRust, primed it with Rust Encapsulater, then gave it a top coat of high-temp caliper paint.

For installation, make sure you keep the engine mounts just loosely fastened, as it will make it easier to align to the engine.  Also ensure you are using new bolts to mount the subframe back to the chassis.  These are high torque bolts and this is a critical connection.  I added a dab of blue Loctite as added peace of mind.  I then wheeled the assembly under the front of the car and raised it using the transmission scissor jack.  It was surprisingly easy to line everything up and torque down.  With the engine mounts tightened down, I could now remove the upper engine hoist, allowing it rest in its normal configuration.

From there it’s just a matter of connecting all the items you previously removed.  Of course this time I installed the steering fluid lines with the appropriate amount of new OEM crush washers.  Hopefully your match marks on the column and pinion lined up properly, mine didn’t.  The result was discovered after a test drive, where I found my steering wheel cocked slightly to the left during straight ahead driving.  Fixing that is a simple removal of the wheel and re-indexing (be sure to make match marks, as you must rotate the wheel to access the Torx bolts securing the airbag.)

The photos below show the completed subframe reinstalled with the steering gear, and lower control arms.  The anti-sway bar has yet to be reinstalled.

Completed Subframe

Before reinstalling the airbox and alternator cooling duct, you’ll need to reinstall the serpentine belt, fill the engine with oil, and then fill and bleed the power steering.  Doing this with those items in place is nearly impossible due to the poor positioning of the power steering fluid reservoir found under the intake tract.  I used less than a bottle of Redline PS Fluid, first filling the reservoir then cranking the engine and sawing the wheel back and forth to bleed out the air.  A little top off was required, but it takes surprisingly little fluid.

Quite the job right?  After the car was back down on the ground I took it for a test drive.  I could feel an immediate difference in the front suspension, everything was a bit tighter, newer feeling.  I also had a bit of an alignment issue, which felt as though I had a little toe-out.  Despite not adjusting the tie rods, you’re bound to have movement in the rack from its original position, however minimal.

Post-Track Inspections and Repairs

Following my first track day with the M3 Sedan, I placed it back on jack stands for my standard post-track inspection.  If anything is going to loosen or break, your best chance of finding it is immediately after a flogging on the track.

I should note that during a few slow speed drives around the paddock at TWS, I kept hearing a squeaking sound.  It was rev-matched to the rotation of the wheels, so it was either at the wheels/hubs or the rear axles.  A quick visual didn’t reveal anything, and eventually the sound subsided.  I should be thanking my lucky stars, because the sound was coming from the Torx bolts that fasten the inboard CVs to the differential stubs.  Several of them had loosened and backed out enough to rub the CV rubber boot.  My first clue was a bit of grease flung on the brand new blue anodized Turner lower control arms.

Obviously this could have been disastrous had the CV become unfastened completely from the differential, especially at the 130+ mph attained at TWS.  I neglected to grab any photos of the issue, so you’ll have to imagine what I’m describing.  To make sure they wouldn’t back off again, I used the impact wrench with a very long extension to tighten all the bolts accessed through the wheel well, with the wheel removed obviously.

Damaged ThreadsWhile I was at the rear, I also noticed that the left lower shock mount bolt had loosened.  I went to tighten it up with an 18mm ratcheting wrench, only to find it stripped.  I had previously discovered some thread damage on the trailing arm, which I thought I had solved by running a tap into the threads.  Unfortunately the threads were damaged beyond simple repair, with about 10mm of thread being completely wiped out.

A slightly longer bolt might have been the cheap and easy fix, but at the cost of reduced thread engagement.  To properly repair this would require an insert or HeliCoil.  I’ve had to make HeliCoil repairs on parts before, such as my Moroso oil pan and the pan mounting holes of my S50.  The principle is simple: drill out the old damaged threads, re-tap the hole with an up-sized tap, then thread in the HeliCoil insert which reproduces the original size threads.  Taping New ThreadsThe inserts are literally coils made of stainless steel.  The kits can be found at most auto parts stores or Fastenal, except in the thread pitch which I needed.  Fortunately they are available on Amazon or elsewhere online.  The complete kit comes with the required tap, inserts, and a tool for threading in the insert.  You must provide the appropriately sized drill bit and tap handle.

The photos below show the damaged threads and taping the new ones (after drilling out, not shown.)  Make sure you cut in a few millimeters at a time, then backing out the tap and cleaning out the hole with some compressed air.  Since this is a blind hole, all the metal shavings will just begin to pile up inside otherwise.

HeliCoil Insert ToolWith the new threads cut, I could now insert the HeliCoil thread restorer.  The insert is wound up on the inserting tool, then held against the surface of the hole.  Then it is screwed into the hole using a tap handle.  This part can be a bit tricky, as you try to engage the insert in the newly cut threads.  Fortunately I got lucky and it went in the first time, unlike my multiple trials with the Moroso pan.  There is a little tang at the end of the coil that the inserting tool grabs on to rotate it.  This tang is notched at the point it bends off from the coils, so that it can be easily snapped off once the coil is fully inserted.  I used a simple flat punch and hammer to knock it loose, then some compressed air to blow it out of the hole.

The photos below show the HeliCoil inserted with the tang still in place and with the tang punched out and in my hand.  And finally some photos of the completed work.  The results are restored threads that are just as, if not stronger than the original.

HeliCoil Inserted Tang Removed

Bolt Reinstalled Job Complete